I used the following instructions to make this (making the letters pockets instead of the area surrounding them).
Monday, March 31, 2014
Project CNC - Success
Finally a successful cutting operation!!! See below for a picture. Used Inkscape to generate text image and imported vector file (.svg file from Inkscape) to MakerCAM to generate tool paths and G-Code tocut out pockets for the letters.
I used the following instructions to make this (making the letters pockets instead of the area surrounding them).
I used the following instructions to make this (making the letters pockets instead of the area surrounding them).
Location:
Plainfield, IL 60544, USA
Saturday, March 29, 2014
Project CNC - RIP for the Rotary Tool
Parting out Dead Rotary Tool |
I was finally able to get my desktop CNC mill to run well enough, with a new carbide end mill, to finally level out the bed. First, though, I had to replace the bed I thought was MDF with actual MDF (turned out that what I thought was thin MDF was really Hardboard which does not mill well).
I generated G-Code to level the bed
with SketchUCAM and then fed it to my mill using Universal G-CodeSender – and it worked great. Well...., except for setting my feed
speed and depth of cuts poorly (I set it up for multiple passes
cutting down only 0.5mm each pass, down to 2mm – so at least 4
passes). Leveling the bed ended up taking about 20 hours – due to
my not optimizing my settings but since I was in bed sick I wasn't
too concerned. After the leveling was done I was able
to cut out a layered pocket for milling PC boards (I put it in the
upper right corner of the bed).
Since I finally had a flat and level
surface to work from I figured I could start cutting out some 2D
shapes: stars, squares and circles. These ended up working fine (can't find my pictures though).
Finally, I thought, it's time to cut out something real. I decided I'd cut out some 2D figures for my daughter. Surprise --- my $15 "Tool Shop"
Rotary Tool finally gave up. Even after completely dis-assembling it (cleaning all dust and corrosion, at least twice) I finally gave up
trying to repair it. I eventually realized that my hours of work, trying to repair this tool, are
worth more than the $20 cost of a new tool for the spindle. So... I
ended up buying a "Cut Out" Tool from Harbor Freight. After discounts
and a coupon it only cost me about $18. It is a bit larger, heavier and more powerful (3.2A instead of 1.5A). So, as a result, I've had to modify my tool mount to fit
the Cut Out Tool. At present it is holding steady (with the help of a few zip ties - I am currently re-designing the Z-axis to make it stiffer/more stable and allow more travel).
Work Holding:
New Tool - Chicago Electric Cut Out Tool |
Work Holding:
Not wanting to have to keep putting
screws into the bed I wanted a way to secure materials so I could
mill them without the piece moving or being dragged by the end mill. Tape definitely didn't work, push pins didn't work,
couldn't find any clamps that would work (tried binder clips, etc).
I finally settled on using T-Nuts on the bottom of the MDF bed.
This, of course, involved making holes through the bed, as well as
countersinking holes on the back side of the bed for the T-Nuts.
- T-Nuts #6-32 screw size
- 7cm x 7cm grid
Currently every thing is working as it is supposed to. I writing some G-code to callibrate the steps per mm for each axis as well as determining the optimal feed rate and depth of cut for MDF and Acrylic.
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